Raising an Obelisk: Part 4
by Rick Brown
Reprinted from the Number 54, December 1999 issue of Timber Framing.
On Sunday, August 29, we filled the box with sand and finished
the ramp. Granite blocks and gravel buttressed the sand box. Late
in the day the obelisk was laid with its center of gravity over the
pivot block on the bearing wall. Next day, we rigged the obelisk,
tensioned the 3-in. steering ropes and began to lower the stone.
Portal captains Wyly and Andy directed two teams made up of
students from the Massachusetts College of Art and National
Guardsmen from Hanscom Air Force Base. Through the 4x5-ft.
portals on either side, the sand was symmetrically removed with
hoes to a line of workers who carried the sand away in baskets.
The sand had been preheated to 160 degrees and delivered (still
hot) absolutely dry to assure free flow. As sand was removed, the
sand remaining inside the box flowed downward toward the portal
consistently maintaining an angle of repose of 35 degrees. We used
this natural slope to support the weight of the obelisk, and the fluid
quality of the flowing sand to gently rotate the obelisk to the
turning groove. As the sand flowed out of the sand box, two
symmetrical slopes formed a ridge down the center of the box in
line with the obelisk, and as the ridge descended, the base of the
obelisk came down with it, and the pillar gradually rotated around
the pivot block above. We had learned from our models that when
sand is removed even one scoop at a time, the obelisk moves in
turn. This provided very precise control of the process.
After every five degrees of rotation, Jim Kricker measured the
profile of the sand to record the relationship between the angle of
repose and the position of the obelisk. By the end of the day we had
reached 45 degrees. Mark Lehner observed that this was already
greater than any of the previous attempts and things seemed completely
under control. Looked like a good time to stop for the day.
On Tuesday, we continued lowering the obelisk, knowing that
rotation beyond 45 degrees would entrain rope stretch. The distance
from the pivot block above to the turning groove on the
pedestal below had been calculated by taking the distance from the
base of the obelisk to its center of gravity (14 ft., 1 in.) and then
adding an allowance for rope stretch based on our testing plus a
generous safety factor. (Overshooting the turning groove cannot be
corrected and therefore was not an option.)
The workers on the
hoes maintained tremendous control on the symmetry and the
sand flow. Every scoop had an effect on how the obelisk moved.
The actual placement of the symmetrical hoes in relation to the toe
or heel of the obelisk was critical in controlling rotation versus
forward slippage as the stone moved closer
to the final 75-degree angle. Casual removal
of sand could result in disaster. Our
obelisk team remained focused and slowly
piloted the stone onto the stair-stepped
bearing wall at 75 degrees, resting on 20
in. of sand directly above and in line with
the turning groove. Coming in 20 in. high
meant that we had had far less rope stretch
than we anticipated. The sand had carried
a greater load than we had expected. Hurrah!
We did not overshoot the target.
Now the brake-release method would
be put to use. The two brake release teams
were led by Al Anderson and Jim Kricker,
while Grigg Mullen and I went inside the
sand pit (facing page) to remove the final
20-in. cushion of sand between the obelisk
and the pedestal stone. Simultaneously,
the two ends of each rope were released in
small increments, repeated by the next
pair of ends until all three sets of ropes
had been equally released. This cycle of
release was repeated again and again as the
sand was removed and the obelisk slid
down the 75-degree pitch of the bearing wall until it came to rest
in the turning groove. The brake release method was very safe and
verified our guided rotation theory.
The next morning, we removed the saddle and the steering
ropes from the obelisk and the brake logs. We packed up our tools
and went home until our return 10 days later for the final pull.
During that period, the sandbox and remaining sand were removed.
The obelisk rested safely in the turning groove and against
the bearing wall, fully rigged and ready to be raised the last 15
degrees. When we returned, on a beautiful, crisp, clear fall day,
nearly 200 eager pullers from the Massachusetts College of Art,
Fletcher Quarry, Hanscom Air Force Base and the film company
joined the obelisk team to complete our task. We spent the morning
on final layout of pulling ropes. Two opposed lateral brake
lines led from a central harness at the pyramidium to deadmen at
the sides, and two brake lines led aft to the brake logs. Four
forward pulling lines gathered into a single braid at the harness.
The braid would avoid any twisting caused by unequal line pull.
Our experience in Aswan demonstrated the importance of having
a unified pulling force. The creation of such a team reenacts a
significant feature of Egyptian building history. Pulling the obelisk
to 90 degrees is a delicate operation. At 75 degrees, the obelisk has
a high and forward center of gravity. After the initial pull towards
upright, the load diminishes rapidly. At 86.5 degrees, the obelisk
develops a forward motion. Lack of attention might result in the
ultimate disaster. We invited the Guild's Joel McCarty, an expert
in on-the-spot group management, to bring his hand-raising experience
to direct an on-site pulling school. Using our 6-ft., 300-lb.
concrete obelisk, the pullers learned fingertip control and experienced
firsthand the physical principles necessary for the job.
The pull would be divided into two parts. The first would bring
the obelisk from 75 to 86.5 degrees, to be held there with a
propping wedge dropped down between the shaft and the bearing
wall. The second pull would bring the obelisk to 90 degrees. Joel
organized his trained pullers into four teams of 28 people, each
team on one rope, standing (for safety) about 100 feet ahead of the
obelisk. Grigg Mullen was nominated Single
Voice to direct the 112 pullers. Al Anderson
and Jim Kricker, our brake and alignment team,
released tension on the rear brake lines simultaneously
as the 112 pullers tugged the obelisk
off the bearing wall. Laura and I lowered the
propping wedge between the bearing wall and
the back of the obelisk to hold the space we
gained as the obelisk moved higher and higher
to the crucial 86.5-degree angle. Single Voice
gave the word to release the lines to give the
pullers a rest before bringing the stone to vertical.
Grigg then surveyed the site, refocused the
troops and called the final pull. All 112 pullers
pulled as one while the brakemen eased off
tension on the rear brake ropes. The obelisk
moved with the grace of a magnificent bird and
without a single sound gently came to rest on
its solid base. Our hand-raising Egyptian-style
was now complete. -RICK BROWN
Rick Brown teaches at the Massachusetts College
of Art in Boston. His last adventure with NOVA
and the Timber Framers Guild unfolded last year
at Castle Urquhart in Scotland,
where he organized the precision casting of 14,000
pounds of lead to be mounted on the throwing arm of a fixedcounterweight
trébuchet. PBS's "Medieval Siege" will air February 1,
2000, and "Pharaoh's Obelisk" will air February 8.